Wednesday, October 21, 2009

A lot of problems.

After some tests in open space, I have seen that the movements of the "quadcopter" become very unstable as after sometime it tends to yaw to the left. I have tried several times to calibrate the "quadcopter", but without success. I have checked again all the components to see if could find any trouble. I have also checked that all the data provided by the MikroKopter-Tool were within the expected values but everything was fine. The next step is to upgrade the Firmware of FlightCtrl to the latest version.

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